Restoring & Upgrading a 1960's Stanley Utility Knife! (And Also Adding a Spring Action & Cutaway!)

by haroldpiercebuilds in Workshop > Metalworking

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Restoring & Upgrading a 1960's Stanley Utility Knife! (And Also Adding a Spring Action & Cutaway!)

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Hello everyone!!

In this Instructable I'll show you how I cleaned up & upgraded a vintage Stanley Utility Knife.

Finding a good USA-made knife these days can cost upward of $100 so I decided to show that while not the same, on a limited budget you can have both an aesthetically pleasing and functional tool!

I also thought it'd be cool to add a spring to help the blade return a little smoother and a cutaway to show off the spring action!

Supplies

The Utility Knife:

1960's Stanley Utility Knife

Cleaning & Polishing

Sandpaper (I used 320-500 grit)

Steel Wool (I used 000-0000)

Upgrades:

Small Spring (I got this one out of a scrap DVD player)

Phillips Head Screw

Tools Used:

Flat & Phillips Head Screwdriver (for the main body screw)

Low Torque Drill

Drill Bits (sizes 1/16 & 1/8)

Automatic Center Punch (for hole layout)

Needle Files (I used a triangle, round, & half round)

Needle Nose Pliers (for the spring)

Razor Blade (I used this to clean out the spots that the sandpaper missed)

Finding a Good Utility Knife to Upgrade/restore

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For this project, I chose a 1960's Stanley 10-099 that I had laying around.

Both the simplicity of the knife (only 4 total parts excluding the blade) and the fact that you can pick up these vintage USA-made utility knives for under $10 makes this the ideal candidate for this project!

Main Body Cleanup

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After some experimentation with a palm sander and belt sander, I decided to remove the paint by hand sanding to ensure the removal of as little material as possible.

Blade Slide Cleanup

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All of the nooks and crannies were hard to get at with sandpaper and steel wool, but I wasn't too worried about it looking perfect, and I ended up liking the patinaed blackwash finish!

Drilling Holes for the Spring Upgrade

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After roughly seeing where I needed to drill the holes for the spring, I marked the hole locations with a center punch and then drilled them with a 1/16 drill bit.

Drilling Holes for the Cutaway - Don't Make the Same Mistake I Did

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For the first (and ugliest) hole, I roughly marked out the hole locations with a center punch and then proceeded to drill a pilot hole with an 1/8 inch drill bit. After trying to upsize the hole with a 7/32 bit, I realized that it was walking around too much because of the interference with the rib on the opposite side, risking both damaging the surface finish and resulting in a terrible looking hole. I then decided to use a 1/16 bit to drill a much smaller hole before upsizing to only an 1/8 hole, hoping to correct this with the needle files.

Making the Cutaway Look Somewhat Presentable

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After connecting the holes with a triangular needle file, I tried my best to make the top and bottom surfaces parallel with the flat side of the half-round file before rounding the corners with the round file.

Final Sand & Polish

What the title says! I continued sanding it up through the grits, finishing with #000 and #0000 steel wool to give it a work-satin finish.

Final Results!

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Overall I'm pretty happy with how it turned out and would love to hear any thoughts and/or suggestions on how I could further improve it!

Thanks for reading, and I hope this inspires you to build something cool!